First Response / SYN-Seal Well Recap

PROBLEM ENCOUNTERED:

THE OPERATOR LOST RETURNS (25-30 BBLS) ABOVE THE WILCOX FORMATION. THEY ARE WANTING TO TOH TO START DRILLING THEIR CURVE.

PRIOR APPLICATON:

CONVENTIONAL CALCIUM CARBONAE, GRAPHITE AND GENERIC FIBER (60 PPB SWEEPS) SET ACROSS THE LOSS ZONE WERE UNSUCCESSFUL. 500 BBLS OF TOTAL MUD WAS LOST IN 2 DAYS.

PRODUCT APPLICATON:

TURBO-CHEM RECCOMENDED AND MIXED AN 80 BBL CONTAINING 40 PPB FIRST RESPONSE AND 10 PPB SYN-SEAL. THIS PILL WAS SPOTTED ACROSS THE LOSS ZONE (6,100’-7,100’) AND A “SOFT SQUEEZE” WAS ENACTED, UNTIL DESIRED PRESSURE WAS ACHIEVED. POOH TO PICK UP ASSEMBLY FOR LATERAL.

RESULTS:

THE OPERATOR TRIPPED BACK INTO THE HOLE THROUGH THE LOSS ZONE WITH NO LOSSES AND CONTINUED TO BOTTOM (10,100’) DRILLING AHEAD AT FULL DRILL RATE TO TD (17,810’). THE WELL WAS SUCCESSFULLY COMPLETED 4 DAYS LATER. TURBO-CHEM’S INNOVATIVE FIRST RESPONSE/SYN-SEAL COMBINATION WAS EXTREMELY SUCCESSFUL INALLOWING THE OPERATOR TO SOLVE MAJOR LOSS EVENTS AND COMPLETE THE WELL WITHOUT FURTHER MUD LOSSES AND COSTLY DOWNTIME.

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