B.F.S. Well Recap

PROBLEM ENCOUNTERED:

THE OPERATOR WERE ENCOUNTERING LOSSES AT 35-40 BBLS. /HR. WHEN DRILLING INTO THE AUSTIN CHALK.

PRIOR APPLICATON:

THE OPERATOR PUMPED SEVERAL COMPETITORS PRODUCTS CONTAINING GRAPHITE, FIBER, CALCIUM CARBONATE AND MICA WITH NO SUCCESS. ATTEMPTS WERE MADE USING A COMPETITORS 2 PRODUCT BLEND CLAIMING A “WIDE PARTICLE SIZE RANGE”. THE LOSSES INCREASED AFTER PUMPING THESE PRODUCTS.

PRODUCT APPLICATON:

TURBO-CHEM MIXED AND PUMPED AN 80 BBL PILL CONTAINING BFS. THE PILL WAS SPOTTED AT 8,800’-9,000’. THE WELL WAS SHUT IN AND A SOFT SQUEEZE WAS ENACTED.

RESULTS:

TURBO-CHEM’S NEW INNOVATIVE BFS PRODUCT WAS ABLE TO ALLOW THE OPERATOR TO GO BACK TO BOTTOM WITH NO LOSSES. AT 11,471’ MINOR LOSSES WERE SEEN AND THE RIG IMMEDIATELY PUMPED A 15 BBL SWEEP CONTAINING 25 PPB OF BFS. ONCE THE SWEEP HIT THE FORMATION, THE LOSSES STOPPED. THE OPERATOR WAS NOW ABLE TO DRILL TO TD (16,950’) WITH NO FURTHER LOSSES WHILE PUMPING MINIMAL BFS SWEEPS.

Print This Page

Endless hours of Engineering and Technology have gone into perfecting each of our products and services. For immediate information on any of our products call 1-800-259-7838.

Contact Us